Press release on 16591 Hampi express
accident at Penukonda on 22/05/2012 at 3.15 hrs.
This
association wish to submit the following facts to your esteemed news paper for
publication.
The railways before conducting an
enquiry, hastly declared that loco pilot ignored the home signal without
analyzing the reasons for the incident. Both the home signals for lines coming
from Dharmavaram and Sathyasai Prasanti nilayam towards Penukonda are somewhat
close and the Hampi express coming from Dharmavaram first sights the signal
from Sathyasainilayam and only when very close to Penukonda sights the
concerned signal. Following are the reasons leading to accident.
1).
In the said accident involved Guntakal loco pilots were working only up to
Dharmavaram from Guntakal till 2009 and later it was extended to Bangalore and
Bangalore Loco pilots spell of run was extended from Dharmavaram to Gundakal increasing
the total working hours to 10 if right time, increasing fatigue. The
parliamentary standing committee on safety recommended 8 hours duty in 2004 and
railways rejected it.
2).
The Gundakal based Loco pilots have to work train towards 6 directions like
Bangalore, Solapur, Gundakal, Hubli, Renigunta and Secundrabad. Similarly
Bangalore Loco pilots have to work towards Gundakal, Arasikare, Mysore, Erode
and Chennai and they happened to work in a particular direction only once in 30
or 40 days and familiarity of rail road is lost. To save 2 or 3 sets of crew
railways extended the run of Loco pilots and invited this accident.
3).
The WDP4 Loco involved in accident was in long hood direction where the
visibility from driving cab is very poor. The railway board specially ordered
the originally twin cab Loco from GM Motors as single cab and done away with
the turning table that were available at all junction stations during steam
period with seant regard to safety.
4).
The railway rule insist to work 6 nights continuously in a week which is beyond
human capacity. The research wing of railway the RDSO recommended long back 2
continues duty in a week, but railway rejected.
5).
The weekly rest for Loco pilots are only four 30 hours and five 22 hours and
railways in recent past tightened the crew links with five 22 hours weekly rest
which is insufficient. Since now as days railways creating economy by not
filling up of vacancies meager 30/22 hours weekly rest is denied to keep the
wheels of the nation moves. Out of the total sanctioned strength of 60, 000
Loco pilots and assistant loco pilots in Indian railways 17, 000 are kept
vacant but the vacancies of the ruling class bureaucracy is 100 % full.
6).
Lastly according to rule points of any station are to be normally set towards non
occupied line, but at Penukonda points were set towards occupied line and this
rear collision happened.
L. MONY
6 comments:
Yes Dear Sir This analysis is 100% true and the reasons are the cause of accident...
Yes Dear Sir This analysis is 100% true and the reasons are the cause of accident...
Good article published in HINDU
A good article published in THE HINDU daily
A good artical published in THE HINDU
Hats off to L.Mony for bringing Loco Pilot problems on Newspapers. I personally feel that Longhood working of WDP4/G4 should be banned, being the main cause for this accident. The same could have been avoided if S/hood working....
Post a Comment